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Water Treatment
Water Treatment > Quality
Water Solutions > Operational Issues
> Evaluating Treatment Costs
Water utilities work hard to balance several treatment
goals at once, often while coping with hard-to-treat waters. Coagulant regimens
evolved through trial and error may accomplish these goals, but may not be as
cost efficient as possible. Economic issues concerning coagulant use affect many
other plant factors, including other chemicals used (e.g., filter aids and those
for pH control and alkalinity) and residue outlays.
In evaluating coagulant cost, consider all relevant cost
factors, including coagulant and co-coagulant dosage, pH adjustment, cationic
and anionic polymer, other chemicals used, sludge disposal and backwash water.
Here are examples of how several plants lowered
treatment costs and improved performance by altering their coagulation
programs.
- A Midwestern utility treating river water wanted to hold filtered water
turbidities below 0.1 NTU and reduce chemical usage. To do so, it switched
coagulants from alum to ferric sulfate and then to a high basicity PACl/polymer
blend. The last option lowered treatment costs by $12.88/MG, held filtered
turbidities below 0.08 NTU on average, and eliminated the need for lime and
cationic polymer. Filter run lengths also increased 30%.
- A plant accessing both lake and river water treated the lake water with
a PACl/polymer blend and the river water with a combination of ferric sulfate,
PACl and polymer. In seeking to simplify operations and reduce cost, it switched
to a high basicity PACl. The new PACl performed at least as well as the other
coagulants on both source waters, met the goal for easy operation, and reduced
cost by 35% for river water and 31% for lake water by sharply cutting coagulant
and soda ash usage.
- A plant treating river water changed coagulant from ferric sulfate to an
alum/ polymer blend and then to a PACl in order to lower residual processing
and disposal costs and reduce caustic consumption. The new coagulant halved
chemical residue volume, cutting sludge disposal costs 44%, and reducing caustic
consumption more than 80%. Total treatment costs dropped 55%.
- A plant using alum to treat river water could not meet its clarification
goals when water temperature dropped to 45? F in the fall. It switched to
a PACl, which eliminated cold water problems. Although PACl dosage was 85%
less than that of alum (liquid basis), settled turbidity was halved, filtered
water turbidity decreased, and filter run lengths improved by 12 hours. Cold
water treatment costs fell by 12%.
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